Just recently rebuilt this bike from the ground up a few weeks ago. Well for the most part. Motor wise I replaced everything it needed. I've been messing with jetting for mid-range since the bike doesn't have the power of my 2006 yz125. Seemed like I got is pretty good. It doesn't have good bottom-mid but top end is awesome. Typical 125 I guess. Well I felt like I had it running good, so I decided to tell my buddy on his 04 rm125 which is ported to do some drags with me. On the second run, (running the bikes to 6th then slowing down), I did pull from him til I hit 6th and then lost power. Bummer! well no big deal..its only a 2 stroke. Thank god I made the switch back to them!
I pulled the piston out and this is what it looked like today. There was aluminum built up on the nikasil at the very top of the cylinder and some on the head. No scaring to the walls, head is all cleaned up now and the aluminum just came right off the nikasil.
Jetting INFO-The bike from the factory comes with 175 main and has a 172 in it. The friend I got the bike off of used to run 50/50 race/pump in the bike at 50:1 and I'm running 32:1 pump gas. So I'm guessing she's lean. Maybe igntion is advanced. No pinging from the motor..that I can tell anyways. Runing Maxima Castor 927 oil.
This was the second time on the bike since build. First was at the track and second was trail riding with my wife and friends. Figured I could get some jetting figured out that I was having problems with at the track.
Here are the pics of the piston


